View Single Post
  #4  
Old 01-Jun-2004, 22:03
mike916 mike916 is offline
Registered Forum User
Bevel Head
 
Posts: 86
Join Date: Dec 2003
Mood: Neutral - but only maybe. 1994 Duc 916S1, 2006 Duc Sportclassic 1000 Sport
Problem now sorted - on checking I found a small oil leak from the crank breather gasket, which I've been meaning to fix for ages, was running down the back of the engine and getting into dodgy some very dodgy connections which plugged straight into the old style switch. New switch fitted that connects directly into the loom without the old style link wire and a new seal fitted on breather unit and the problem is now well sorted.

Thanks for the info received - goes to show switches on Ducatis do not always pack up - it was the wiring!sing:
Quote+Reply